- Joined
- Feb 11, 2006
- Messages
- 8,028
- Location
- Jacksonville
- Bike
- GL1800 R1200RT NC700
- 2025 Miles
- 006216
After a problem the weekend before last that stranded me for the first time since I have owned my RT I believe I have set things to right. The problem made its presence known Saturday before last when the RT quit on me without warning 15 miles from home. It was 95F and I had been riding for 3 hours. It just shut off while accelerating through 70 mph onto an interstate entrance ramp. On the shoulder I got it started but it was sputtering and cutting out over 3000 rpm so rode 2 miles to a safe place to assess things. I had to traverse either of two long bridges to get home and did not trust the bike to continue running so I retrieved my bike on my utility trailer. The next day it ran fine during a 30 mile ride in the cool of morning. During the week I couldn’t find anything obviously wrong and sort of chalked it up to a stick coil breaking down under heat and load. The problem fit the symptoms of a bad upper coil, which is not unknown on higher mileage 2005-2009 boxers. Last Saturday I headed out on it to get a photo tag and at 30 miles it quit in the predawn darkness. On the center standt would start and idle and rev in neutral but as soon as I dropped it in gear it quit. A light bulb in my head lit up…. The side stand was up but it acted like it was down. I dropped the side stand and tried to start it in gear and it started in gear with the clutch in and the side stand down. It was if the switch was reversed in operation. I couldn’t ride it home with the stand down so I cycled the side stand up and down several times while wiggling the play out of it and managed to keep it running while in gear with the stand up. I gingerly rode it home, grabbed the NC and went for the photo tag. When I got home I examined the side stand switch in light of day. It was loose and just a gentle push popped it off the locating stud. Simple fix. The $2 circlip that holds it in place on the stud was gone allowing the switch nearly to fall off. It must have been working intermittently for a week. The local dealership had the clip and washer in stock and these secured the switch and fixed the problem. Rode it 92 miles today with temps 99-100F and it purred.
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